4.0 Summary of Major DCISC Review Topics, 18th Annual Report - July 1, 2007 thru June 30, 2008
4.17 Outage Management
4.17.1 Overview and Previous Activities
The DCISC monitors PG&E’s outage plans, actions, and results in the following ways:
- Review of outage safety evaluations and plans
- Regular Fact-finding meetings to discuss planned major modifications, inspections, maintenance and activities
- Regular reports from PG&E at DCISC Public Meetings on outage plans and outage performance, noting any special situations or problems affecting safety
- Visits to DCPP during outages to monitor the Outage Coordination Center, Control Room and activities of interest
- Reviews of documentation and reports of outage activities such as steam generator tube inspections, major equipment problems, and events affecting safety
PG&E completed its thirteenth Unit 1 & 2 refueling outages (1 R13 & 2R13) during the 2005-2006 reporting period. Since the DCISC began review of this subject in 1990, outage management performance has steadily improved as shown in the table below. PG&E expects its outages can routinely run in the high-twenty to low-thirty day range.
Other outage indicators also are showing continuous improvement. With the exception of anomalous 1R9 radiation levels, radiation exposure and personnel injuries have been generally declining in the last three outages as follows:
| Outage Duration (days) | Collective Radiation Exposure (person-Rem) |
Personnel Safety (recordable injuries) |
||||
|---|---|---|---|---|---|---|
| Outage | Unit 1 | Unit 2 | Unit 1 | Unit 2 | Unit 1 | Unit 2 |
| R10 | 40.4 | 29.5 | 162 | 108 | 2 | 1 |
| R11 | 30.3 | 33.5 | 138 | 125 | 4 | 2 |
| R12 | 77.5 | 57.0 | 149 | 98 | 5 | 0 |
| R13 | 41.0 | 38.8 | 116 | 74 | 5 | 3 |
| R14 | 29.8 | 68.9 | 103 | 226 | 6 | 3 |
The DCISC reviewed the following during the previous reporting period.
- Outage 2R13 Safety Plan
- Outage 1R14 Work and Safety Plans
- Readiness for Restart Program
- Outage 1R14 Results
The DCISC concluded in the previous period that the DCPP 1R14 Outage Refueling Outage results were good with relatively low collective personnel radiation dose and human error, and no significant nuclear safety concerns or events.
4.17.2 Current Period Activities
The DCISC reviewed the following outage-related topics during the current period:
- Outage 1R14 Safety Schedule Changes
- Outage 2R14 Major Work, Safety Plan & Results
- Outage 2R14 Containment Integrated Leak Rate Test (ILRT)
- Lessons Learned in Outage 2R14 and Outage 1R15 Plans
Outage 1R14 Safety Schedule Changes
The DCISC Fact-finding Team met with Dennis Peterson, DCPP Outage Director, at the August 2007 Fact-finding Meeting (Volume II, Exhibit D.2, Section 3.5) to discuss the three outage safety plan changes in Outage 1R14. The DCISC initially became aware of these changes at its June 13-14, 2007 Public Meeting (Reference 6.6).
DCPP prepares an Outage Safety Plan for each refueling outage. The purpose of the plan is to provide information on outage safety requirements and risk areas for the plant staff. In order to assess outage safety impact, the Outage Safety Plan is referred to prior to making major schedule changes. Plants can be susceptible to variety of situations challenging safety during shutdown conditions. PG&E’s outage safety program is designed around three major concepts:
- Prevention of any accident-initiating event
- Mitigation of an accident before it potentially proceeds to core damage
- Control of radioactive material if a core damage accident should occur
The Outage Safety Plan provides background information for the logic contained in the Outage Safety Checklists. The checklists provide the logic used to develop the Outage Safety Schedule. The Outage Safety Schedule, along with the checklists, ensures the equipment and plant conditions assumed in the shutdown abnormal procedures are met. The shutdown abnormal procedures provide guidance for providing passive core cooling and key system restoration.
There were five potential changes from the 1R14 Outage Safety Schedule as follows:
- Offsite start-up power was lost for approximately 55 minutes to both units due to a failed Morro Bay-to-DCPP transmission line. Unit 1 was shutdown in No Mode with all fuel offloaded to the Spent Fuel Pool (SFP). Auxiliary power had been cleared for maintenance, and 230 kV offsite power was supplying start-up power. Emergency Diesel Generator (DG) (EDG) 1-3 was cleared for maintenance. Upon loss of 230kV/start-up power, EDGs 1-1 and 1-2 auto-started as designed and powered their loads. SFP cooling, not automatically loaded on the EDGs, was manually started by the operators within five minutes per procedures. Unit 2 continued to operate normally. There was a six-hour schedule impact on the outage but no safety impact on the plant.
- The Outage Safety Schedule included all three EDGs as available for core reload; however, due to emergent maintenance, EGD 1-3 was not available. All other on-site and off-site power sources were available and energized with required cross-tie capability. There were no impacts on outage activities or plant safety.
- The Outage Safety Schedule had all three EDGs and both off-site power sources required for reduced Reactor Coolant System (RCS) inventory Refueling Outage procedure in which, after shutdown and a cooling period, reactor coolant is lowered below the hot and cold legs, permitting work to be performed in a relatively dry environment. The operation is a relatively high-risk condition due to the potential for loss of cooling.">mid-loop operation; however, EGD 1-3 had not been returned to service. Except for EGD 1-3, all power sources were available and energized. Station management approved continuing outage activities with EGD 1-3 out-of-service. There were no impacts on outage activities or plant safety.
- EGD 1-2 was declared inoperable for approximately 85 minutes due to an oil leak on a pressure gauge fitting on the lube oil system. The fitting was tightened and the EGD declared operable following a satisfactory test run. All other required power sources were available and energized. There were no impacts on outage activities or plant safety.
- A Component Cooling Water (CCW) System isolation valve was found to be leaking, temporarily adversely affecting the ability to provide clearance on CCW Pump 1-3. The valve was repaired and the system returned to service. There were no impacts on outage activities or plant safety.
Each of the changes was documented, evaluated, and approved by plant staff and management prior to proceeding with work affected by the change. The evaluation includes comparison with the Outage Safety Checklists for required operable and available components and systems. Except for the first change above (loss of off-site start-up power), none of the changes reduced Defense-in-Depth (DID) below the checklist minimum. The first change was evaluated as reducing DID below checklist values but having little or no safety impact. The event will be added to the Outage 2R14 Safety Plan as operating experience.
DCPP performed a Root Cause Analysis (RCA) of the first change (loss of off-site power). The root cause was identified as the 230kV loop relay protection scheme not being designed for an unanticipated voltage transient in the output signal supplying the protection relay for a breaker. A contributory cause was an in-service failure of a non-ceramic insulator near the Morro Bay Switchyard. The Corrective Action to Prevent Recurrence (CAPR) was to reconfigure the breaker protection relays in the Mesa and DCPP switchyards to establish a 16 millisecond (one cycle) time delay in their protection scheme. This has been completed.
The unanticipated voltage transient has been determined to be applicable only to the DCPP and Mesa switchyards. The cause does not apply to the 500kV system.
The DCISC Fact-finding Team believes these evaluations and corrective actions were appropriate.
The five potential Outage 1R14 Safety Schedule Changes were documented, evaluated and dispositioned properly by DCPP staff and management as required by DCPP procedures. The evaluations appeared to be satisfactorily analyzed for safety impact. One of the five changes actually reduced Defense-in-Depth below pre-determined conservative checklist minimums, but it had no actual safety impact on the plant.
Refueling Outage 2R14 Major Work, Safety Plan & Results
The DCISC Fact-finding Team (FFT) met with DCPP and received a presentation on DCPP Refueling Outage 2R14 at the following meetings:
- August 21-22, 2007 Fact-finding Meeting (Volume II, Exhibit D.2, Section 3.5)
- October 24-25, 2007 Public Meeting (Volume II, Exhibit B.3)
- April 16-17, 2008 Fact-finding Meeting (Volume II, Exhibit D.9, Section 3.3)
- June 25-26, 2008 Public Meeting (Volume II, Exhibit B.9)
The 2R14 overall outage results were as follows:
| 2R14 Goals | 2R14 Results |
| Zero Nuclear Safety Events | Zero |
| Zero Disabling Injuries | Zero |
| > 2 Recordable Injuries | Three |
| Zero Human Performance Clock Resets | Zero |
| Zero FME Significant Events | Zero |
| > 66 Days Breaker to Breaker Schedule Duration | 68 Days 22.5 Hours |
| > 5 Day Power Ascension | @lt; 5 Days |
| 100 Power < 90 Days | Met |
| Dose Goal 256.7 Person-Rem | 226 Person-Rem |
Although DCPP did not attain its outage duration or recordable injury goals, the overall outage was considered by DCPP and the FFT to be successful. Notably, there were no nuclear safety events. There were 18 changes to the Outage Safety Schedule, one of which was considered notable but not a safety concern.
Major work items in the outage were as follows:
- SG replacement
- Containment fibrous material elimination - part of the containment sump replacement
- Pressurizer weld overlay - a U-2 specific task with high dose exposure
- Recirculation Sump modification - to be based upon U-1 experience
- Integrated Containment leakrate test - done every 15 years over approximately 36 hours, a variety of contingency plans are in place, containment inaccessible above certain pressure
- Charging Pump 2-3 replacement
- Charging Pump 2-2 rotating element replacement
- Reactor Coolant System make-up controls upgrade
- 4kV Bus F load cables and cubicle hinge wire replacements - a continuing project, this is the last U-2 bus
- Service Cooling Water System chemical cleaning
- Reactor Vessel Head inspection - a routine task, last time before head replacement
- Main Generator inspection - a routine task
- Condensate Storage Tank floating roof replacement - to address degradation
- Diesel fuel oil storage tank cleaning - a routine task done every 10 years, with the diesel fuel off loaded from the underground tanks to tanker trucks
The Outage Safety Schedule Change Process is a controlled method to handle changes to the pre-established outage schedule for having safety equipment and sources available. The one notable change was isolation of Component Cooling Water to the Containment Fan Cooler Units (CFCUs) which could impact containment temperatures affecting personnel working conditions; however, no safety problems were identified. Examples of other changes were:
- High wind watch while on Start-up Power
- Emergency Diesel Generator (DG) (EDG) maintenance performed during core offload
- Main bank transformer oil leaks requiring clearance of auxiliary power supply
- Residual Heat Removal (RHR) Pump leak
- ILRT activity schedule change
The DCISC believed this process was effectively utilized and was in part responsible for DCPP’s maintaining nuclear safety throughout the outage.
As is typically done following each outage, DCPP developed a list of “lessons-learned” to enhance performance in future outages. The 2R14 list included the following major lessons learned:
- Improve outage schedule logic and reviews
- Simplify the scope deferral process
- Make containment equipment hatch closure requirements consistent
- Increase training for fuel movement upender operators
- Increase qualified maintenance resources for emergent work
- Improve pre-job planning in Mechanical Maintenance
- Add a planning prioritization scheme in Maintenance Planning
- Add manual valves to Safety Injection test loop to accommodate check valve leakage testing
Approximately 200 days into Cycle 14 prior to the outage, Chemistry identified and monitored a fuel failure according to DCPP procedures. Radiochemistry results indicated one or two open fuel defects. This resulted in ramp rate restrictions to protect the fuel, plans for outage in-mast fuel sipping and fuel repair activities, and enhanced 2R14 foreign material search provisions. Following the sipping, one once-burned core peripheral assembly was found to have a single fuel rod with a defect. The defect consisted of a corner rod separated into two pieces; however, field inspections could not identify the failure mechanism. Because of the nature of the defect, the assembly could not be re-constituted and was removed from service. This required a minor core redesign and the use of six additional assemblies to maintain core symmetry with the affected assembly removed. The redesign resulted in a small impact on full power capability and minor adverse changes to core operating limits (peaking factor margin reduction by 1.7 and Axial Flux distribution initially more negative by 0.6).
The fuel vendor, Westinghouse, and DCPP are performing a root cause analysis expected to be complete by June 2008. In addition to the fuel defect, DCPP discovered unexpected internal wear in an instrument guide tube which was also under investigation. The DCISC should request a presentation on this analysis and investigation at its June 25-26, 2008 Public Meeting.
DCPP’s Outage 2R14, an outage of unusually large scope with four Steam Generator replacements, was performed successfully overall. As expected by DCPP, a single fuel rod defect was identified as well as an instrument guide tube with unexpected internal wear. Both are under investigation which the DCISC should continue to monitor.
Outage 2R14 Containment Integrated Leak Rate Test
The DCISC Fact-finding Team met with Meagan Wilson, Associate Engineer and Containment Integrated Leak Rate Test (ILRT) Day Shift Test Lead,at the May 20-22, 2008 Fact-finding Meeting (Volume II, Exhibit D.10, Section 3.12) to review the ILRT completed in Outage 2R14. This is the DCISC’s first review of this test.
The DCPP Containment, like all nuclear power containments, is designed to provide near-leak-tight containment of any radiological materials in the building which might otherwise escape during normal, off-normal or accident conditions. NRC regulation 10CFR50, Appendix J contains requirements for containment leak rate testing generally on a ten-year basis; however, certain exceptions are permitted. The last test of DCPP Unit 2 was 15 years ago due to a five-year extension by NRC. NRC is considering going to a standard 15-year period based on the good performance of the industry in maintaining containment leak tightness. The test was performed in accordance with industry standard ANSI/ANS (American National Standards Institute/American Nuclear Society) 56.8-1994, “Containment system leakage Testing Requirements (Absolute Method, Mass Point Analysis, Leakage Stabilization Criteria, Termination Criteria).”
The DCPP Containment contains a net free volume of 2.55 million cubic feet and has a design pressure of 47 psig. The Containment has a Technical Specification maximum design basis leak rate of 0.1 weight /day used for accident calculations.
The ILRT was performed by ILRT, Inc., a specialist in ILRT testing, and required 42 hours (vs. a projected 36 hours) and included the following steps:
| Step | Time Required (hours) |
| Pressurization | 7.5 |
| Stabilization/Troubleshooting | 16.08 |
| ILRT itself | 10.00 |
| Verification Test | 4.00 |
| Depressurization delay | 0.75 |
| Depressurization | 3.00 |
| Unrestricted access restored | 0.66 |
Pressurization was begun at 1810 hours on April 2, 2008 at an average pressurization rate of 8 psi/hour using 17 compressors with a rated capacity of 27,500 cfm. The test was performed at almost 46 psig (end of test) with the following results:
- Measured leak rate = 0.0132 wt./day (0.0144 wt./day at the upper 95 confidence level)
- ILRT Acceptance Criterion = 0.075 wt./day
The DCISC Fact-finding Team received a copy of the test report “Periodic Reactor Containment Building Integrated Leakage Rate Test Final Report,” dated April 3&4, 2008. The report was thorough and informative. The test team generated many lessons-learned to improve the Unit 1 ILRT in early 2009.
The DCPP Outage 2R14 Unit 2 Containment integrated Leak Rate Test (ILRT) was performed successfully. All test acceptance criteria were met. The measured leak rate was approximately one-sixth of the acceptance criterion.
1R15 Outage Plan
DCPP presented its Outage 2R14 lessons-learned and its plans for Outage 1R15 at the DCISC June 25 & 26, 2008 Public Meeting.
Outage 1R15, scheduled for January 26 – April 16, 2009, is similar to Outage 2R14, except for the following major scope areas which differ:
- Flow Accelerated Corrosion - 30” Main Feedwater Header
- Conversion of the Pressurizer Safety Valves to Steam Seated Valves
- Reactor Vessel Head Inspection
- Diesel Fuel Oil Storage Tank Cleaning
- Replacement of Containment Building Penetration 43
The Safety Plan for 1R15 is essentially the same as that during 2R14; however, the 1R15 Safety Plan will incorporate the lessons learned form 2R14. The infrequently performed evolutions during 1R15 are the same as during 2R14 and include:
- Initial Drain Below 25 Pressurizer Level
- Integrated Safeguards Testing
- Reactor Startup
- Mid-loop Operations for Vacuum Refill
- New SG Performance Testing
- Integrated Leak Rate Test
Key 1R15 challenges include:
- Industrial Safety and Human Performance - akin to 2R14
- Outage Schedule Development/Optimization
- Maximizing and Managing the Pre-Outage Work Window
- Laydown Area Coordination
- Equipment Load-in and Load-out
- Integrated Leak Rate Test
- Reactor Vessel Head Inspection
- Integrating Other Containment Work Scope with the SG Replacement Project
- Site Parking Space Constraints and Traffic Management
- NEXIS/SAP
- Planning for 2R15 (Early October 2009) with Scheduled Reactor Head Replacement
Outage 1R15 has somewhat less scope than 2R14 due to no sump modification work being required, that work having been previously performed.
4.17.3 Conclusions and Recommendations:
- Conclusion:
- DCPP’s Outage 2R14, an outage of unusually large scope with four Steam Generator replacements, was performed successfully overall. As expected by DCPP, a single fuel rod defect was identified as well as an instrument guide tube with unexpected internal wear. Both are under investigation which the DCISC will continue to monitor.
- Recommendations:
- None